Hi Jag,
* the Port wing station has been MRF( 9740)again due to the display monitor blacking out.
* the Stbd Main battery charger was going in to recondition mode but has been reset, please keep an eye on it.
* MRF 9750 was entered for Port Aft Main with a coolant leak, the leak is actually from the thermostat & Brody/ Matt are aware.
* all our fire equipment was inspected on the 18/06/2024 but the powder extinguisher at the base of the ladder in the Port engine room was not stamped on its yellow tag. An MRF was entered.
* maintenance conducted 500 hr genset service on the 20/6/24 & found a raw water leak behind the Starboard genset. The have asked that we do daily inspection behind both gensets.
* please keep an eye on the Port Fwd Mains coolant level, it's been acting a bit odd. It seemed slightly high when cold on the first weekend, I removed one litre of coolant to get it back to the cold fill line. It then dropped below the cold fill line after first run on Monday so I added 300 ml. I have photo documented the levels at different temps/ time of day & sent an email through to Brody if you could read the email. I have cleaned up the cap thread on all header tanks also.
* all airconditioning units were professional cleaned during our swing.
* There are some spare batteries for hand held radios in the chart draw. They are all fully charged. Please be aware that we are not to leave any batteries on charge when we are not onboard to supervise